minilathe22
Established Member
I have been using my Union Graduate with what appears to be the original 3/4HP Newman 3 phase motor, running it through a VFD. I found on larger diameter work although the VFD can reduce the spindle speed to 100RPM, the spindle can be stopped too easily, as it does not have any reasonable torque.
I recently started using a bowl saver, and found this to be a particularly slow process with the motor coming to a complete stop unless I was very careful.
So I decided to upgrade the motor to a more powerful one, and came across this motor on ebay.
It is more powerful at 1.5HP (1.1kW) but will also give more torque at lower RPM because it is a 6 pole motor, and runs at 930RPM no load speed (at 50Hz) compared to the old motor which was a 4 pole motor (1425RPM at 50Hz).
The new stepped pulley did not have a keyway, and I did not think that one small grub screw would hold it securely enough. So I carefully hacksawed and filed away part of a keyway, but could not reach easily into the centre of the pulley. I opted to trim the key supplied with the motor until it all fit together. Hopefully with a belt drive there will not be too much shock applied to the key/keyway. I then tapped and drilled another securing screw, with a plain hole drilled in bottom of the outer pulley to give access for the drill, thread tap and screwdriver. I also tightened the provided grub screw aswell, which went down into the void left by the missing part of the key. dab of loctite on both threads to keep it from shaking loose.
The motor did not have mounting legs, and is actually designed to be mounted on a flange at the front. This proved not to be a problem though, as it had several M8 threads already tapped into the body that I used. Both sides of the bolts have cork mounting material to hopefully absorb sound and vibration.
Not much looks different now its all installed. I had to adjust the pulley tensioner, as I think the centre of the motor spindle is now slightly higher than the old motor arrangement. I am slightly concerned about motor cooling, as there is only 15mm or so between the fan intake and the side of the lathe casting, so it probably cannot draw air as easily. I will have to monitor how hot the motor gets during use.
I have found the motor can run fine at 120Hz, although it will have alot less torque at this speed. This means in theory on the highest ratio pulley setting I can have a spindle speed of up to maybe 3000RPM, hopefully it has enough torque for a buffing wheel at this speed.
Depending on how hot the motor and VFD heatsink get, I will decide whether a cooling fan is needed to circulate air within the lathe body.
I then sold the old motor complete with the old pulley and bolts to attach it to the motor plate, helped to reduce the cost of the conversion a little bit. Now I need to get my rev counter working again to see how slow it will go!
I recently started using a bowl saver, and found this to be a particularly slow process with the motor coming to a complete stop unless I was very careful.
So I decided to upgrade the motor to a more powerful one, and came across this motor on ebay.
It is more powerful at 1.5HP (1.1kW) but will also give more torque at lower RPM because it is a 6 pole motor, and runs at 930RPM no load speed (at 50Hz) compared to the old motor which was a 4 pole motor (1425RPM at 50Hz).
The new stepped pulley did not have a keyway, and I did not think that one small grub screw would hold it securely enough. So I carefully hacksawed and filed away part of a keyway, but could not reach easily into the centre of the pulley. I opted to trim the key supplied with the motor until it all fit together. Hopefully with a belt drive there will not be too much shock applied to the key/keyway. I then tapped and drilled another securing screw, with a plain hole drilled in bottom of the outer pulley to give access for the drill, thread tap and screwdriver. I also tightened the provided grub screw aswell, which went down into the void left by the missing part of the key. dab of loctite on both threads to keep it from shaking loose.
The motor did not have mounting legs, and is actually designed to be mounted on a flange at the front. This proved not to be a problem though, as it had several M8 threads already tapped into the body that I used. Both sides of the bolts have cork mounting material to hopefully absorb sound and vibration.
Not much looks different now its all installed. I had to adjust the pulley tensioner, as I think the centre of the motor spindle is now slightly higher than the old motor arrangement. I am slightly concerned about motor cooling, as there is only 15mm or so between the fan intake and the side of the lathe casting, so it probably cannot draw air as easily. I will have to monitor how hot the motor gets during use.
I have found the motor can run fine at 120Hz, although it will have alot less torque at this speed. This means in theory on the highest ratio pulley setting I can have a spindle speed of up to maybe 3000RPM, hopefully it has enough torque for a buffing wheel at this speed.
Depending on how hot the motor and VFD heatsink get, I will decide whether a cooling fan is needed to circulate air within the lathe body.
I then sold the old motor complete with the old pulley and bolts to attach it to the motor plate, helped to reduce the cost of the conversion a little bit. Now I need to get my rev counter working again to see how slow it will go!