niall Y
Established Member
It must have been beginners luck , last time, because when I turned some 18mm diameter ferrules and rings, from some 20mm nickel silver rod; I don't remember the hassle I have encountered this time around.
I spent the whole of today making 4 x 18mm outside dia. x 6mm long ferrules, They were admittedly slightly more complicated,in design having two inner diameters. of 12.7mm and 14mm with the step down about 2mm from the end.
The struggle seemed to start from the off. Cutting away a section with a hack-saw was tough going and took forever. I set it up in my ER32 chuck on the lathe and attempted to drill out with a centre bit but it just wouldn't work i used a small cobalt bit instead to drill out enough to take a revolving centre.
I then tried to reduce the outer diameter to a tad over 18mm. The cutters all seemed to struggle to give a smooth surface and I had to resort to emery to get rid of the ridges Drilling out the centre with an 8mm cobalt bit first followed by a 12mm one, again was really hard going with the lathe shaking and juddering despite applying lots of cutting fluid.
I even resorted to annealing the workpiece, hoping for an improvement, during the next stage. I used a tungsten tipped boring bar to widen the drilled centre and was getting some nice shavings. But the lathe juddered so badly I had to attach a G cramp to hold the tool post down to the carriage. Things did start to improve from hereon in, though I found I had to sharpen the parting tool every time I made a new cut. At the end of the day I feel I've struggled a lot, for so little reward.
I spent the whole of today making 4 x 18mm outside dia. x 6mm long ferrules, They were admittedly slightly more complicated,in design having two inner diameters. of 12.7mm and 14mm with the step down about 2mm from the end.
The struggle seemed to start from the off. Cutting away a section with a hack-saw was tough going and took forever. I set it up in my ER32 chuck on the lathe and attempted to drill out with a centre bit but it just wouldn't work i used a small cobalt bit instead to drill out enough to take a revolving centre.
I then tried to reduce the outer diameter to a tad over 18mm. The cutters all seemed to struggle to give a smooth surface and I had to resort to emery to get rid of the ridges Drilling out the centre with an 8mm cobalt bit first followed by a 12mm one, again was really hard going with the lathe shaking and juddering despite applying lots of cutting fluid.
I even resorted to annealing the workpiece, hoping for an improvement, during the next stage. I used a tungsten tipped boring bar to widen the drilled centre and was getting some nice shavings. But the lathe juddered so badly I had to attach a G cramp to hold the tool post down to the carriage. Things did start to improve from hereon in, though I found I had to sharpen the parting tool every time I made a new cut. At the end of the day I feel I've struggled a lot, for so little reward.