All sorted
When I opened up the motor casing there was piles of fine dust inside ! Explains why on start up yesterday it had started blowing some fine dust out which I had thought was just dust that had settled on the rim and been blown off.
Vacuumed it all out and blew off all parts of the motor with the air line, checked the brushes which were 6mm x 8mm and 25mm long, seemed to be plenty of life left in them as I had to compress the springs a fair bit when refitting them. No signs of wear or burning on the bit where they contact (armature or commutator ? Can you tell I'm not technical :lol: ).
I had checked the paper bag pre-filter when I took it off and it seemed intact, and the main cartridge filter seemed pretty clean inside it but I blew it off with the airline anyway before refitting with a new paper bag filter just to be sure.
Reassembled and all worked fine, running much cooler now too and the suctions better.
I think the main cartridge filter must have had a knock when I was brushing excess dust off of the paper bag filter which I do occasionally, and affected the seating and sealing of the base of the cartridge where it meets the motor casing, allowing some dust up into the casing and affecting the motor operation ? It wasn't obviously not properly seated when I took it off, but I guess it wouldn't take much to cause a problem, so made sure to reseat it firmly when reassembling.
Been using it on and off for a couple of hours this morning and seems to be fine now thankfully
Thanks for all the help and suggestions guys, appreciated.
Cheers, Paul