MarkAW
Established Member
I have a Charnwood Cabinet saw and the dust extraction on it is poor. All the dust drops out the bottom onto the floor, but it's not a bad saw otherwise. After seeing someone mention on here how they solved it, I thought I'd post a description of my project to help anyone else
Here's my table saw opened up via 4 bolts/screws on the top side panels:
You'll see it's all open to the floor and the 100mm inlet turns into something much smaller inside
That internal pipe is fitted to the internal blade guard with an even smaller square cutout inside:
I needed to be careful any modifications or additions didn't foul the tilt and height mechanisms that drop the motor below the top cabinet at their extremes:
So I ordered a big mouth extraction hood from Axminster and deliberated for quite some time how best to fit it.
In the end I:
And a few more pictures in progress for reference:
I intend to get some magnetic sheets to cover the large gaps at the tilt mechanism holes front and back and haven't cut anything, so haven't got a verdict on how well it performs yet. Should be a lot better.
Here's my table saw opened up via 4 bolts/screws on the top side panels:
You'll see it's all open to the floor and the 100mm inlet turns into something much smaller inside
That internal pipe is fitted to the internal blade guard with an even smaller square cutout inside:
I needed to be careful any modifications or additions didn't foul the tilt and height mechanisms that drop the motor below the top cabinet at their extremes:
So I ordered a big mouth extraction hood from Axminster and deliberated for quite some time how best to fit it.
In the end I:
- Cut some plywood the same size as the internal of the top cabinet. Cut out the size of the hood from that, but specifically in a position for it to fit so that the motor would drop into the opening of the hood.
- Cut that plywood in half to allow easy fitting. (It was possible to get the hood in through one of the sides with a bit of fiddling, so no need to lift anything heavy.)
- A little cut out for the cable clip (a welded on nut)
- Removed the old dust port connection and marked out and cut (using a jigsaw with metal blade) a bigger port to allow a 100mm hose to pass through. Filed and sanded.
- Added a plywood ramp to help funnel some of the dust into the hood at the same angle as the hood. (This took some careful measuring)
- Remove and cut off one side of the blade guard and the small port (I would have taken the guard off completely, but thought it best to provide some protection from projectiles hitting the plastic hood) I left two faces continue so I could bend them together to provide a continuous protection surface. It also meant I didn't need to fiddle with the alignment of the riving knife as the blade guard was fitted with it using bolts. Be careful which you undo. There's two at the back for the alignment that you want to leave untouched
- Fitted the 100mm pipe and screwed down the hood (don't drop any screws, bolts or tools at this point, they'll be tricky to retrieve)
- Put some draft excluder foam tape I had lying around onto the more open spaces around the bottom sides of the cabinet. The goal here wasn't to seal it up, there's plenty of air gaps under the table, it was to focus the airflow from the top down into the hood rather than the sides
And a few more pictures in progress for reference:
I intend to get some magnetic sheets to cover the large gaps at the tilt mechanism holes front and back and haven't cut anything, so haven't got a verdict on how well it performs yet. Should be a lot better.